谭劲旅,陈振富*,刘巍,易灵芝.自密实钢筋混凝土梁阻尼比的试验研究[J].南华大学学报(自然科学版),2010,24(1):102~105.[TAN Jing-lv,CHEN Zhen-fu*,LIU Wei,YI Ling-zhi.Experimental Study on Damping Ratio of Self-compactingReinforced Concrete Beams[J].Journal of University of South China(Science and Technology),2010,24(1):102~105.]
自密实钢筋混凝土梁阻尼比的试验研究
Experimental Study on Damping Ratio of Self-compactingReinforced Concrete Beams
投稿时间:2009-11-27  
DOI:
中文关键词:  自密实钢筋混凝土  简支梁  振动试验  阻尼比
英文关键词:self-compacting reinforced concrete  simple beam  vibration test  damping ratio
基金项目:
作者单位
谭劲旅,陈振富*,刘巍,易灵芝 南华大学 城市建设学院,湖南 衡阳 421001 
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中文摘要:
      对15根自密实钢筋混凝土简支梁进行了动态测试实验,实验结果表明:随着自密实混凝土强度的提高,其阻尼比降低;随着自密实混凝土梁的固有频率的增大,其阻尼比减小;随着自密实混凝土梁配筋率的提高,第一阶固有频率下的阻尼比降低;各自密实钢筋混凝土试验梁的阻尼比基本介于0.5%~1.0%之间.
英文摘要:
      In this paper,fifteen self-compacting reinforced concrete beams are used for the dynamic testing.The analysis of experimental results indicate that: The damping ratio of beams decreases with increasing the self-compacting concrete strength;the damping ratio of beams decreases with increasing the natural frequency and with the self-compacting concrete beams reinforcement ratio increased,the first-order natural frequency of the damping ratio reduces.The damping ratio falls in 0.5%~1.0% for self-compacting reinforced concrete beams of vibration test.
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